Posts Tagged ‘eog resources inc’
Pa. blowout report cites mistakes
Gas drilling incident in western Pennsylvania linked to firm’s corner-cutting tactics.
From staff and wire reports
HARRISBURG – Rig workers’ inexcusable failure to use a second set of pressure-control devices while preparing to connect a natural gas well to a pipeline led to the well’s blowout in western Pennsylvania last month, a consultant’s report said Tuesday.
State regulators, who hired the consultant, quickly ordered all drilling operators to adhere to a set of safety standards designed to prevent another such incident.
“I don’t know any company that would cut corners like this on this kind of well,” said consultant John Vittitow, a Texas-based petroleum engineer.
The company, Houston-based EOG Resources Inc., has used this same tactic on other wells in Pennsylvania, Vittitow said.
“I don’t think they’ll use it again,” he added.
Meanwhile, state Environmental Protection Secretary John Hanger warned that another such incident could mean the end of EOG’s business in Pennsylvania, and insisted state regulations don’t allow EOG’s tactics.
EOG and its contractor, C.C. Forbes Co. of Texas, were given maximum fines of more than $400,000 combined and ordered to take corrective actions, but were allowed to resume all activities in Pennsylvania on Tuesday after a 40-day suspension of well-finishing work.
EOG operates nearly 300 wells in Pennsylvania.
The blowout happened late June 3 on the grounds of a hunting club in Clearfield County where EOG is drilling a number of wells.
For 16 hours, explosive gas and briny wastewater shot into the air before specialists brought it under control.
Hanger insisted Tuesday that existing regulations do not allow EOG’s tactics because they require companies to obey accepted industry safety standards.
Most companies obey those, he said, but a letter sent Tuesday would lay out in detail what is expected of them.
Gary L. Smith, EOG’s vice president and general manager in Pittsburgh stated in an e-mailed that company officials “sincerely regret that the well-control issue took place.”
Since that time, Smith said, EOG has worked with the DEP to resolve all issues, will implement the new operational procedures outlined in the letter to gas well operators and looks forward to resuming activities.
Marcellus Shale Coalition president and executive director Kathryn Klaber said the new regulations DEP put forth “have already been incorporated by many of our members as part of their regular wellsite operations.”
State Rep. Phyllis Mundy, who is leading the charge for a moratorium on gas drilling in the state, said the $400,000 in fines and 40-day suspension “seems like a pittance … for what was clearly an inexcusable lack of proper procedure to care for the environment and their workers.”
Mundy, D-Kingston, said the incident “reinforces the need to hit the pause button with a moratorium. With this kind of activity, there will always be accidents.
“But with proper laws, regulations, best practice guidelines and inspections in place, we could prevent many of them and be much better prepared to deal with them when they do occur. Those things are not in place at this time, yet we continue to issue new permits. We are simply not prepared to either prevent or react to these incidents.”
Hanger said his agency would redouble its inspection activity with more emphasis on well-finishing work.
Copyright: Times Leader
Pa. stops company’s drilling after accident
The order against EOG Resources Inc. will remain in place until DEP can finish its investigation.
MARC LEVY Associated Press Writer
HARRISBURG — Pennsylvania regulators halted work Monday at dozens of unfinished natural gas wells being drilled by the company whose out-of-control well spewed out explosive gas and polluted water for 16 hours last week.
The order against Houston-based EOG Resources Inc. will remain in place until the Department of Environmental Protection can finish its investigation and until after the company makes whatever changes may be needed, Gov. Ed Rendell said.
The order stops EOG from drilling and hydraulically fracturing wells. It affects about 70 unfinished EOG wells into the gas-rich Marcellus Shale formation.
Another concern was the apparently bungled attempts to notify the right emergency-response officials about the accident. Fines are likely, said Environmental Protection Secretary John Hanger.
Nobody was hurt in Thursday’s blowout in a heavily forested section of north-central Pennsylvania.
The accident shot highly pressurized gas and wastewater as high as 75 feet. The gas never caught fire, but state officials had worried about an explosion and ordered electrical service to the area cut before specialists secured the well at about noon Friday.
About 35,000 gallons of wastewater have been pumped into holding tanks so far, the company said.
Monitors in a nearby spring show signs of pollution, although Hanger said the spring is in such a rural area that it is not viewed as a public health hazard. Officials say they have detected no pollution in larger waterways that feed public water supplies.
The state says the company is cooperating and is supportive of the stop-work order.
Gary L. Smith, vice president and general manager of EOG’s Pittsburgh office, said the company regrets the accident and would continue to work with Pennsylvania officials.
“After the investigations are complete, we will carefully review the findings with the goal of enhancing our practices,” Smith said.
“When all outstanding issues are resolved, we look forward to resuming full operations in Pennsylvania,” Smith added.
DEP officials said the well’s blowout preventer failed, and they were investigating whether the failed equipment was the primary cause.
A blowout preventer is a series of valves that sit atop a well and allow workers to control the pressure inside.
Hanger and EOG said the blowout preventer had been tested successfully by the company on Wednesday morning.
Copyright: Times Leader
West Virginia gas well blast injures 7; flames now 40 feet
VICKI SMITH Associated Press Writer
Published: June 7, 2010
MORGANTOWN, W.Va. (AP) — A crew drilling a natural gas well through an abandoned coal mine in West Virginia’s Northern Panhandle hit a pocket of methane gas that ignited, triggering an explosion that burned seven workers, state and company officials said Monday.
The blast created a column of flame that was initially at least 70 feet high, but the rig operator said the site was secure and the fire was about 40 feet high by late morning.
A team from Texas-based Wild Well Control, a company that specializes in rig fires, will decide whether to let the methane burn or try to extinguish the flames, said Kristi Gittins of Dallas,Texas-based Chief Oil and Natural Gas.
The explosion occurred about 1:30 a.m. in a rural area outside Moundsville, about 55 miles southwest of Pittsburgh, and presents no danger to any structures or people, said Bill Hendershot, an inspector with the state Department of Environmental Protection’s Office of Oil and Gas.
The operation was less than a week old: DEP records show a permit was issued June 2 to AB Resources PA LLC of Brecksville, Ohio.
Gittins said AB Resources is the operator of the well, while Chief has a “participation interest.” It is Chief’s responsibility to drill and complete the well, she said.
Chief’s site contractor, Union Drilling of Buckhannon, had drilled the first 1,000 feet of a second well on the property and was preparing to install surface casing when crews apparently hit and ignited the methane, she said.
Crews had drilled through the abandoned Consol Energy mine before without incident, she said.
Methane is a known risk when working near old mines, and the company typically takes a variety of precautions, including venting systems. Gittins could not immediately say what precautions were in place at this site.
“Luckily, our response team got there quickly, secured the area and evacuated the workers,” she said. “From all appearances, there weren’t any life-threatening injuries, so that’s a good thing.”
The seven workers were taken the West Penn Burn Center in Pittsburgh and were in fair condition, a hospital spokeswoman said.
Five were employed by Union and two worked for BJ Services Co. of Houston, Texas, said Jeff Funke, area director of the Occupational Safety and Health Administration’s Charleston office.
A spokesman for Union in Fort Worth, Texas, did not immediately return a telephone message.
The BJ Services workers were among four that had just arrived on site to place the casing, said Gary Flaharty, a spokesman for the parent company, Baker Hughes Inc. of Houston. The crew runs a safety check at the start of each shift and was just preparing to do that when the blast occurred.
Flaharty could not provide any details about the injured employees but said they’re being treated for burns and are expected to survive.
Funke said OSHA learned of the accident shortly after 8 a.m., and two investigators were being dispatched. However, they cannot enter the site and begin work until the fire is out, he said.
OSHA created a program to deal with gas drilling in the vast Marcellus shale fields about five years ago and has been proactively inspecting sites to ensure compliance with safety regulations, he said. The gas reserve is about the size of Greece and lies more than a mile beneath New York, Pennsylvania, West Virginia and Ohio.
OSHA knew there would be a lot of drilling in West Virginia and Pennsylvania, “and we did our best to get out in front of that curve,” Funke said. “So we’re well-equipped to respond to this.”
About 98 percent of the region’s drilling now involves Marcellus shale, he said.
Gittins, the spokeswoman for Chief, confirmed the company was tapping into the Marcellus reserves. The company has drilled about 75 Marcellus wells in West Virginia and Pennsylvania so far, she said, with about 15 of them in West Virginia.
This was the company’s first major accident, she said.
However, it’s the latest in a string of accidents related to the rapidly growing pursuit of Marcellus gas.
In Pennsylvania, environmental regulators are investigating what caused another well to spew explosive gas and polluted water for about 16 hours last week until it was brought under control.
A crew of eight was evacuated from the Clearfield County site Thursday, but no one was injured. That accident involved EOG Resources Inc. of Houston.
Copyright: The Scranton Times-Tribune
Pa. inspectors looking into gas well emergency
MARC LEVY Associated Press Writer
HARRISBURG — State environmental regulators worked Sunday to get to the bottom of what caused a natural-gas well to spew explosive gas and polluted water for 16 hours last week before it could be brought under control.
Neil Weaver, spokesman for the Department of Environmental Protection, blamed a failure on the well’s blowout preventer, a series of valves that sit atop a well and allow workers to control the pressure inside. Investigators are trying to figure out what caused the malfunction.
The blowout is the latest in a string of accidents connected by regulators to the rapidly growing pursuit of the rich Marcellus Shale gas reserve that lies beneath much of Pennsylvania.
It seems likely the Pennsylvania blowout will enter the debate in the Capitol, where legislators are battling over the merits of an extraction tax and tighter regulations on an industry that has spent several billion dollars and drilled more than 1,000 wells in Pennsylvania in just a couple years.
State Rep. David Levdansky, D-Allegheny, said such oil problems could bring increased interest in a moratorium on leasing public land for gas drilling and a severance tax that could largely fund existing environmental protection and cleanup programs. Levdansky is a leading environmental advocate.
Weaver declined to discuss whether investigators have found anything so far or whether well driller EOG Resources Inc. of Houston committed any violations that could lead to fines or any other penalties.
An EOG spokeswoman said Sunday the investigation into the cause is ongoing, and the company had no light to shed on the blowout.
Crews evacuated the site Thursday night and didn’t regain control over it until just past noon Friday. No one was injured, the gas didn’t explode and polluted water didn’t reach a nearby waterway, officials said.
The blowout sent highly pressurized gas and polluted water 75 feet into the air. Huge tanks were required to cart off chemical- and mineral-laced water collected on the grounds of the private hunting club where the well had just been drilled.
Copyright: Times Leader